Norman with his back to the camera hooks up the knuckle patch to the air hoist while Mike assists. |
Severn Edmonds was in by Thursday afternoon much to our
delight. He has made it his mission to get the Lodge & Shipley 16” lathe
running for the last year, and I can report that we were finally able to make
real actual parts on it this time! Thanks to Severn for sticking with it!
My hope was to start drilling the remainder of the 2” holes
in the front tube sheet this time. I purchased a special hole cutter bit and
adaptor so it could be used in a conventional drill chuck, and arranged to have
Severn borrow the magnetic base drill press from our generous friends at GGRM.
Sadly the adaptor did not fit the drill chuck, so Severn is making up a new bit
of tooling so this can be done in the fall. A person can only plan for so much,
we continue to fight on.
Dave Anderson continues the needle scaling marathon. |
Kirk Baer makes cleaning locomotives look good! |
On a happier note, Bob Sims has been quietly converting our ancient
D&RGW box car into the steam department tool car. I was pleased that some
of our tooling was moved out of my overloaded tool “dumpster” and into the car.
Hank and Dave got a long steel table from out in the bone yard, straightened
the legs and fork lifted it into the car using Bob’s angular calculations. The
resulting space is a real boon to the steam guys, and will help productivity
greatly given that everything will be at hand, rather than in a messy pile.
Thanks to Bob for sticking with the project and to everyone who helped get us
moved in.
Our boilermaker, Norman Comer was in from Tuolumne, CA. His
efforts were concentrated on fitting the rear tube sheet knuckle patch that
Roger cut out in the spring. This project requires a great amount of fussy
cutting and measuring, and he will hopefully be back after Railroad Days to
finish it up before Cody the Welder is back out in the fall from Cheyenne, Wyoming
to finish all the sheet renewal work.
Severn Edmonds at the helm of the 16" lathe. |
Hank and Severn drilling out rivet holes in the new wrapper patch using the magnetic base drill. |
Throughout the course of the weekend my dad was content to
hang out in the climate controlled zone of the Pullman sleeper and catch up on
his reading, and take the occasional nap. This was a nice change from the day
to day of his regular home life. He did wander over to the shop periodically to
check on our progress, but given that a heat wave was on, and the interior of
the building was hotter than the hinges of hell, we only saw him briefly. To be
honest I wouldn’t have minded joining him in the car from time to time myself.
Traditionally, the summer sessions are our least patronized
as far as volunteers go, but I am happy to say that things are looking up.
Kirk, Dave, Larry, Charlie, Burr, Mike, David, Hank, Duane, Bob, Norman and
Severn did accomplish a great deal, and they have my gratitude, and the
gratitude of the Board.
Saturday night everyone was invited once more to Kirk and
Debbie’s for the evening meal. It was a nice gesture, and a great way to get
everyone in one place at the same time for conversation and storytelling. This
social aspect is what I enjoy most about coming up to Portola, so kudos to you
guys for facilitating this "team building" event, we hope we can do it again soon!
A big thank you goes to Gail McClure for designing and
printing the new 165 “Heavy Metal” t-shirt for sale in the gift shop. Please
pick one up next time you are at the museum! And thanks also to the switch crew
lead by Steve Habeck who had the engine and tender spotted right where we wanted
it. I know it’s not always easy to move stuff around in that yard, kinda like
one of those sliding tile puzzles given the amount of equipment we own.
Sunday morning finally arrived, so dad and I moved out of
the Pullman, and we headed out the gate. We returned by way of Pine Grove so I
could drop a chunk of railroad iron off at my property. Taking Carson Pass over
into California, I managed to avoid Highway 80 entirely, which was great. Dad
was likely happy to get back home. I took a pause for the cause and headed back
out on the road to LA. I arrived late that evening and decompressed a bit
before collapsing. Unenounced to me, a week of sanding and painting ceilings
lay ahead; something I really didn’t plan for. - JCA